Sunday, April 21, 2024

Husky 2 gallon compressor repair

 My compressor crapped out about a week ago.  After I took the cover off, I discovered a circuit board inside with a DC motor.  The fuse on the circuit board was blown.  After making a trip to Lowe's to get 3A 1-1/4 inch AGC fuses, I replaced the fuse. When I powered the compressor it blew the fuse again. 


I suspected a burned out motor, but didn't see any indication.  I made sure the compressor was unplugged and removed the cover again.  The small circuit board seemed simple enough, as it contained only a bridge rectifier and a capacitor and fuse. 


I removed the screws holding the circuit board to the chassis and turned the board over to look. 


I traced out the circuit, as shown below: 


The input ac power is fused, then run to the power switch. From there the AC line goes through a 100 psi pressure limiter switch.   After this the AC line and neutral are applied to a diode rectifier. The rectified DC is filtered by a small capacitor and then applied to the DC motor. 

The motor resistance was 13 ohms which seemed reasonable.  I clipped one of the wires to the motor to isolate the circuit from the motor.  Then I used my multimeter in diode voltage mode to check the diode bridge.  One of the arms of the diode bridge was shorted.  The bridge is a KBPC610, which I found I could order 10 pieces from Amazon for $8. 


When I received the replacement diode bridge, I soldered it in and tested the compressor, but it didn't work.  After some troubleshooting I found that one of the AC input connections to the board had broken off under the insulation.  After fixing this the compressor ran ok.  I carefully spliced and insulated the wire I had cut to the motor.  Then put everything back together, making sure that none of the wires was in danger of getting caught by the small axial fan that is under the cover. 

I hope the air compressor will keep running. I bought it about 15 years ago at Harbor Freight in Houston. 

Wednesday, April 17, 2024

ESP-32 data logger (1): micro SD logger design

 I am backing away from the battery charger project because I need to complete another project to continue.  So far I've been using a pencil and paper to record battery charge and discharge curves.  I am going to automate that data acquisition process using a ESP-32 microcomputer.  The first attempt will be to store the data to a micro SD card.  The second version will be to use WIFI to store the data on thingspeak.com. 

I have an ESP-32 development board that I bought off of amazon.com. (link).  It's a pretty sophisticated MCU.  I program it using the Arduino IDE.  The development package is 38 pins.  A diagram of the different pin functions is shown below



The test circuit for the micro SD logger is shown below.  The circuit will be powered through the development board USB port.  I order the micro SD card module from amazon.com (link).

click to enlarge

The circuit is wired up on solderless breadboard as shown below, The ESP32 dev board is on the left and the micro SD reader is on the right.   The first experiment will be to simply write some data into the micro SD card and read it back. 





Friday, April 12, 2024

12V 7.2AH SLA battery (4): LM317 battery charger test

 When I originally tried a LM317 circuit, I used the circuit I found at this link.  The LM317 charger circuit is quite popular and can be found all over the web. The circuit I'm using differs from that at the above link in that I added a 100 ohm resistor in the base of the 2N3904 current limiting transistor. I did this to protect the transistor. The circuit is design for a charge voltage of 13.8V and a charge current limit of 0.75A. 

Click to enlarge

The charging circuit works as follows: 

  • The LM317 regulator controls the voltage drop between the power source on the left and the battery on the right to maintain 1.25V from the VO pin to its ADJ pin. 
  • The regulator voltage is set by VO = (1+(RV1+R5)/(RV1+R5+R4)*1.25V)
  • The battery charge voltage is set to 13.8 volt. Given the values in the schematic, this corresponds to RV1 = 2.52Kohm
  • R6 and Q3 form a foldback current limiter circuit. The current limit cuts in when the voltage at R6 reaches about 0.6V.  If R6 = 0.82 ohms (four 3.3 ohm resistors in parallel), then the current limit will be 0.6V/0.82ohm = 0.73A. 
  • In actual operation with a discharged SLA battery, the circuit will initially attempt to regulate the battery voltage at 13.8V but current limiting would cut in, resulting in constant charge current as the battery charged.  As the battery charge voltage approached 3.8V the current limiting would cut out and battery charge current would fall while the charge voltage remained constant. 
I built the charger circuit 


After building the circuit, the LM317 charger was tested as shown in the photo below.  In the upper left is a 23V source taken from the unregulated side of a 13.8V power supply. The charger circuit is in the lower left while a voltage and current monitor for the battery is in the lower right while the battery itself is in the center right. 

click to enlarge

The initial test of the LM317 charger is shown below.  A problem with is test is that the voltage was not set to 13.8V as required.  The voltage was set to 13.4 volts. The battery fails to charge fully and final battery charge voltage settles at 13.3 volts.  

click to enlarge

The test will be conducted after adjustment of the set voltage to 13.8V. 



Thursday, April 4, 2024

Craftsman 10" bandsaw 113.244513 (5): Testing new lower blade guide (updated)

 I installed the new lower guide into the Craftsman saw, as shown in the photo below.  There were minor issues and one major issue as noted in the photo and the list below the photo.

click to enlarge


  • There is interference between the left side of the thrust bearing axle and the case. This is easily fixed by cutting the ends of the axle down.
  • There is possible interference between the right blade guide and the case.  Fix by cutting the guide length down. 
  • Change all the set screws to Allen style headless screws.  This will help reduce places to snag when installing the sawblade.
  • The thrust bearing is not centered on the blade.  For now I will install a shim under the lower blade guide support to move the guide over about 1 mm. 
The saw runs fairly well, with some noise. Once I get the above issues on the lower guide fixed, I'll replace the wheel bushings with ball bearings, and replace the worn tires. 

UPDATE: 
I bought a bottom style 10-24 tap on Amazon.com for $3.  It cleaned out the set screw holes very well.  Now the set screws don't jam and it's easy to feel when the screw contacts the blade guide.   I also shortened  the thrust washer bearing axle and the two blade guides.  Now there is no interference of those features with the case.  

I printed a set of shims to use under the lower guide support to center the thrust bearing  on the blade. The shims were nominally 1mm, 0.5mm, and 0.25mm thick.  Upon actual 3D printing, each shim was 0.13mm or so larger than nominal.   The 1mm and 0.5mm shims together seemed to center the blade on the bearing the best. 

The photo below shows the shims after 3D printing.



The photo below shows the guide installed with notes on latest changes.

click to enlarge





Craftsman 10" bandsaw 113.244513 (4): Lower blade guide redesign (results)

This lower guide replaces Craftsman Part 69174  in the 113.24413 model bandsaw. 

I did the lower blade guide redesign in Fusion 360.  See the diagram below with changes noted.  I increased the material volume around the blade guide set screws and added holes normal to the layer plans to accommodate 2mm reinforcing screws. The holes for the thrust bearing axle were enlarged to get a sliding fit on the axle, and 3mm set screws were added to hold the axle fixed.

click to enlarge



I 3D printed the guide out, using black PLA, 100% fill.  Because of the black plastic of the guide it is hard to photograph. The photos below show the guide with hardware installed from a front and rear view.  

click to enlarge


Some notes: 
  • I have not used the Cura slicer software to calibrate hole sizes while printing. All holes in the guide were slightly small. I spent a lot of time drilling out holes, experimenting on test pieces to check for correct size. 
  • I was not able to use a tap well for the 10-24 saw guide set screw holes.  The tap bottomed out against the bottom of the blade guide holes. Because of this the set screws tend to jam as they get near the blade guide. That makes it difficult to feel when the set screws are solidly against the guides.
  • The 2 mm tread inserts I used from the bottom for the reinforcement screws were a little tricky to install. I put them on the tip of a soldering iron and melted them into the guide body.  I had to use a screw from the bottom side  to clean out the melted plastic from the from the holes, then install the reinforcement screws from the top side. 
  • I didn't use a tap on the thrust bearing axle set screws, but rather let the screws cut their on threads in the plastic.  I don't think this will be a problem as the screws don't have to be torqued very much to prevent lateral movement of the axle.   Next time I'll use thread inserts to get  better seating on the screws. 
I will be installing the guide in the saw today and testing how well it works. 

Monday, April 1, 2024

Craftsman 10" bandsaw 113.244513 (3): Blade guide redesign plans

 I bought this Craftsman 10" 3-wheel saw in August of 2023 for $10.  At the time, it didn't have the switch key or a blade installed, so the owners just sold the unit for salvage.


I found a switch key for  Craftsman products on Thingiverse.com (link).  I  then  3D printed the key in PLA, The key has to be positioned with the "legs" up while printing, and then the support material under the "head" has to be whittled off, but the switch key functions very well, as shown below. 


The saw needs new tires, but I haven't ordered any yet. I bought a 56-7/8 inch 1/4" 14TPI bandsaw blade (link) for the saw and spent some time trying to tune up the saw.   In the process I discovered that the lower blade guide to the saw was broken.   The guide body, Craftsman part 69174, is cast from pot metal, and broke at an obvious weak spot as shown in the photo below.  I found a Thingiverse.com replacement (link).  The printed out replacement part is shown below.  It was printed in orange PLA with 100% fill.  The hardware for the thrust bearing has been moved to the new PLA bearing  The blade guides were missing in the original part. I used 1/4" bookshelf pins for the side guides. 



The photo below shows the lower guide after installation. The thrust bearing has a groove in its surface and needs to be replaced. 

click to enlarge

The problem with the 3D printed part is immediately apparent as shown in the photo below. The blade guide set screws produce stress that is normal to the 3D printed layers.  The part is weak in that direction and the stress causes fractures parallel to the layers as can be seen in the photo. 


Someone must have experienced this problem and revised the part to be more robust (link).  See screen capture below. 

Another problem to consider is the replacement of the thrust bearing.  See the photo below and the issues list below that. 

click to enlarge



Thrust bearings issues list: 
  1. There is no provision for moving the thrust bearing laterally to center it on the saw blade. The lateral position of the blade is mostly determined by thickness of the bandsaw tires.  I don't know how much of an issue this lack of lateral adjustment will be. 
  2. The current bearing is worn with a groove on its surface.  I found replacement bearings on Amazon.com (link). They are 3mm ID X 10mm OD X 4 mm wide.  I've also found 3mm stainless steel rod to make the axle (link).  I haven't yet found material to make the spacers.
  3. The thrust bearing is difficult to install on the guide. The axle is currently pressed through the guide plastic body.  I don't like guessing the proper diameter to get a good interference fit for the axle.  Also without some sort of installation jig, pressing the axle stresses the plastic guide body and distorts the part. 
My plan for the plastic guide redesign are shown in the sketch below, which is a side view of the guide: 

  1. Extend the material adjacent to the saw guide set screws and add reinforcing screws to prevents cracking of the plastic when the set screws are tightened
  2. Eliminate the interference fit of the thrust bearing axle and make the holes a free fit. Then add set screws to prevent the thrust bearing axle in place. 
  3. Produce the thrust bearing axle spacers using 3D printing, making their lengths asymmetric to keep thrust bearing centered on the saw blade. 
I will import the bearing guide stl file into Fusion 360 and modify it as needed to get a revised part. 



Saturday, March 30, 2024

Duracraft VS-312 Bandsaw restoration (7): operational test of new 3D printed gear

I modified the Fusion 3D model of the motor gear from 10.15mm ID to 10.12mm ID.  I used PLA material for the gear, 100% fill. It took 2 hours to fabricate.

To mount the gear onto the motor shaft, I first used the old gear to find the best position of the gear on the shaft. If the gear is too far up the motor shaft, the belt will wander off the wheel,  if the gear is too far down the motor shaft, the belt will get frayed on its outer edge by the outer lip of the gear.  When I found the optimal placement of the gear, I marked a short stick with a pencil to mark the height of the top of the gear from the saw case. 


To install the new gear, I first boiled some water in a tea kettle, poured it into a disposable cup, then dropped the new part into the hot water to let it expand.  After a few minutes I took the hot gear and tapped in down on to the motor shaft until it lined up with the mark for the proper height.  I had no trouble moving the gear down the motor shaft, it went down with just light tapping with a wooden mallet.


The saw was very finicky to get set up.  The three tension controls interact quite a bit.  After about an hour of getting familiar, I finally got the saw running.  I adjusted the blade position so that the blade saw teeth were slightly off the tires: 

The lower and upper blade guides are definitely worn out,  I'll cover rebuilding the guides later. 

Below is a video of a test cut with the saw:








Duracraft VS-312 Bandsaw restoration (6): wheel alignment study

 I have taken some time to better study the wheel alignment on the Duracraft VS-312 bandsaw. 

The wheel axles are in 10mm bearings with the wheels nominally 1 inch wide (25.4mm).  The axle pins screw directly into the bandsaw casings. 

The left photo below shows the mounting hole in the saw casing, and on the right is a photo of the axle pin partially screwed in.

click to enlarge


The photo below shows an axle pin

click to enlarge


Below is a diagram of the axle pin, showing dimensions: 

click to enlarge

Going from the wheel hub (left side) to the case (right side) are the following sections of the pin:

  1. A slotted screw head
  2. A snap ring the holds the outer wheel bearing
  3. A shoulder to the bearing formed by a 6 mm OD 1mm wide recess
  4. M8 screw threads that screw into the bandsaw casing.
The photo below shows the axle pin installed through a wheel bearing.  The wheel bearing is about 1mm narrower than the bearing area on the pin, as is noted in the photo. This results in 1mm on axial play in the bearing, which I reduced by putting a total of 0.7mm of shim washers between the snap ring and the outer side of the wheel bearing.

click to enlarge

As I originally found the bandsaw, it had two 5/16" washers installed between the saw casing and the pin's bearing shoulder as shown in the photo below.  The washers had a large ID, giving a loose fit around the threads. Also, because of the 6mm slot next to the shoulder, the washers seated poorly when installed. The washers move the wheels outward away from the case by 3mm, which caused the gear wheel of the motor to be far out on the end of the motor axle.

click to enlarge

I ordered a metric E-clip assortment and replaced the poorly fitting washers with a 6 mm E-clip.  I am convinced that this was the way the axles were originally designed to be configured.  The E-clip fits in the slot in the pin and seats well. The distance between the inner side of the wheel and the shoulder on the pin is now reduced to 1mm, moving the drive gear on the motor inwards by 2mm. 

click to enlarge


Another problem I found was that the upper wheel didn't have any washers installed. This results in a 3mm misalignment of the upper wheel in relation to the lower wheels. As designed, the upper wheel has fixed alignment with the other two wheels, but has an adjustment of angular alignment to position the saw blade.  So the 3mm misalignment was likely causing binding when the blade turns.  I have now installed the proper E-clip in all three wheels and I think I should get good alignment of the three wheels with much less friction than before. 



Friday, March 29, 2024

CARI Chess & Amateur Radio Int'l

 I have 2 qsl cards from Tom Palmer whom my dad and I



played chess with.  It shows the Chess Frequency Schedule at the time (1984).  I had the game in my log which disappeared long ago.  I sure would like to play "on air" again.  So all you Hamster out there that love chess give me a call.  my email address is on my QRZ page under KA5VZE.  The same call as my novice call.  I still write down everything that is said to me and may even record.  I only do cw but if someone will teach me to tune up my FT 757- GX for fon I would gladly oblige them.

Try this link also: https://www.kb6nu.com/play-chess-cw

73s Mike Morris KA5VZE

 

Monday, March 25, 2024

12V 7.2AH SLA battery (3): XL4015 buck converter charger

 I ordered step down modules from Amazon.  I bought 3 modules for $11.37 total.  The modules are rated for 5A with outputs from 0.8V to 30V. I haven't measured the dropout voltage but it appears to be slightly more than 1 volt. 



The unit has a voltage regulation adjustment and a current limit function.  I set the voltage at 13.8V and set the current limit to 0.72A, which is 10% of the battery's 7.2 Ah capacity.  After discharging the battery to about 50% state of charge (SOC) I recorded the current and voltage of the battery as it was charging.  See plot below: 
click to enlarge

The current is limited at 0.70A for the first hour or so. Then the current drops exponentially while the voltage approaches a constant voltage of 13.5 volts or so.   This is controlled 2 stage charging.  For a third stage the voltage could be dropped slightly for long term trickle charge.  This seems like a pretty good charger circuit and costs less and $4 for each module. 





Saturday, March 23, 2024

12V 7.2AH SLA battery (2): 1st current limiter

 My initial try at a current limiter is a foldback circuit I used back in the '80s for charging a small battery. See below.  The charging current flows from Vin through Q2 collector to emitter, then through current sensing resistor R2.  When the voltage across R2 reaches about 0.65 volts, then Q1 turns on and robs the base of Q2 of current, limiting the current to 0.65V/R2, in this case the current limit is 0.79A. 


As built the circuit is shown below.  It functioned as predicted, limiting the battery charging current to about 0.78A.  However my lab power supply only goes to 18V and this circuit required 3 or 4 volts to operate properly.  But the real problem was that it was difficult to predict the final charge voltage once the battery current fell off.  This gives a risk of undercharging or overcharging the battery.  I will try a different approach with a LM317 regulator IC.





Friday, March 22, 2024

12V 7.2AH SLA battery (1)

 I bought a 12V, 7.2AH sealed lead acid (SLA) battery from Amazon (link). 


As a reference for the required charging curve I'm using the chart from page 7.38 of the 2023 ARRL Handbook.  See graph below.  For Stage 1 current I use C/10,   for 0.72 A.  Topping charge voltage will be the bottom of the Handbook guide of 2.3V to 2.45V per cell, i.e., 13.8V.  This is in accordance with voltage recommendations on the side of the battery. Float voltage will be 13.5V.  So summarizing: 
  • Stage 1: constant current 0.72A
  • Stage 2: constant voltage 13.8V
  • Stage 3: constant voltage  13.5 V
I am in the process of designing the charging circuit now.  I have ordered some UC3906 Lead Acid charger controller ICs from Amazon (link).  I've also ordered XL4015 based buck converters (Amazon link). These buck converters can be programmed for an output voltage and current limit that will produce multi-stage charging. I'm also thinking of using a LT3652 IC based module (Amazon link)




Duracraft VS-312 Bandsaw restoration (5): final testing fail

 Yesterday I installed the upper and lower blade guides, then mounted the table and did some tests.

  1. The blade guides are worn and need to be rebuilt.  I'm hold off on discussing the blade guides until I start doing their rebuilds. 
  2. The table wasn't hard to install.  
  3. When I tested the saw on random blocks of soft wood, it didn't cut well.  I wonder if I've got the wrong style of saw blade. 
  4. After several minutes of testing the drive wheel started slipping, then stopped working all the way.
  5. I will have to 3D print out a replacement with a smaller size hole and try it again.  I may work on some scheme to add a allen screw locking mechanism.  If I do, hopefully the PLA plastic isn't too soft.



Wednesday, March 20, 2024

Duracraft VS-312 Bandsaw restoration (4): Drive sprocket and belt installed

I did the following work on the Duracraft bandsaw today:
  1. Installed washer shims on the axles of the wheels.  Each pulley required about 0.6 mm of shimming to reduce the side play on of the each wheel on its axle. 
  2. I used silicon grease on each axle to reduce friction and noise.  
  3. I installed urethane bandsaw tires on the wheels.  Not that easy, easier with practice. 
  4. I installed the 56-7/8",    3/8" wide, 6 tpi saw blade.  
  5. I adjusted the tension and blade position using the tension adjustment and camber adjustments on the top wheel.
I ran the saw for about 10 minutes and don't see any problems as yet. 
Now forward to get the blade guides installed. 
Photo of the saw in its current state is below. 

 



Sunday, March 17, 2024

Duracraft VS-312 Bandsaw restoration (3): Drive sprocket and belt installed

 On the Duracraft bandsaw... after checking the alignment of the wheels, I've found that the wheel bearing have about 1mm of side to side play.  I've ordered shim washers that I'm going to use to get the play down to 0.1 mm or so.  

The bandsaw drive belts came in today.  I set up the motor driving the bandsaw drive wheel.  See photo below. 



I pulled the drive sprocket out quite a bit to get proper belt alignment.  I may make a spacer later to get repeatable axial placement of the sprocket. 


The video below shows the operation of motor, pulley and drive wheel. Next task is to install shim washers to reduce axial play.




Saturday, March 16, 2024

Duracraft VS-312 Bandsaw restoration (2): Drive sprocket

 In order to replace the motor drive gear on the Duracraft bandsaw I found a similar part on thingiverse.com for a Craftsman 10" bandsaw. After printing out the thingiverse.com part, it was totally identical to the existing Duracraft part, except Craftsman part mounted on a 0.5" shaft, while the Duracraft part mounted on a 10.0 mm shaft.  

I had to import the thingiverse part .stl file into Fusion 360 and modify its inner diameter (ID) to have an interference fit on the a 10 mm shaft.  Below is the Fusion 360 drawing.  The thingiverse part is in green and my modification for the 10 mm shaft size is in grey.



Making the part was more complicated than I thought it would be.  The accuracy of the hole size of my 3D printer is off, even though the precision is pretty good. I printed a series of test pieces to find the right compensated hole diameter to use.  Printing 4 different diameters at a time I was trying to bracket the proper diameter to use, but it took me four 3D printing runs to find the proper diameter to use.  The stack of test pieces is shown below. 


Eventually I printed out a gear that had a tight fit to the motor shaft. 


The next task is to carefully check the alignment of the wheels and drive gear.  Then if everything is ok, I'll install the belt and check that the motor drives the drive wheel correctly.